Stop tweaking the ground pad prints; start tweaking the I/O prints.
Would you believe QFN ground pad voids could be cut by over 50% with a zero-cost, super-simple stencil aperture modification? Not a mod to the ground pad apertures where the voiding is problematic, just to the I/O apertures? Neither did we. That’s why we did some deeper digging into what we are now calling the “AIM I/O” aperture modification.
In November’s column, we reported a dramatic reduction in voids when QFN I/O pads were left unpasted, and mentioned our technical staff’s observations and ensuing experiments led us to this new void mitigation technique, but we didn’t explicitly describe the I/O aperture design. It’s a simple overprint at the toe of the pad.
In an experiment we will present at IPC Apex Expo next month, we took three different MLF devices and applied four levels of overprint to each. Overprints were measured in simple distances: 0 (1:1 with pad), 10, 20 and 30 mils, extending from the toes (FIGURE 1). These small overprints should pull back readily in the reflow oven without forming solder balls, especially with Pb-free solder paste.
FIGURE 2 shows the effect of the overprinting on void formation on three different sizes of QFN: 16, 32 and 48 I/O. The drop in voiding is dramatic, and we were astonished at the results.
Voids were consistently reduced by one-third or more simply by increasing the volume of solder paste on the I/O pads. The next obvious question is, What is causing these dramatic, repeatable voiding reductions? Unfortunately, peering inside a convection oven during the reflow process to observe what’s happening in real-time on minute solder deposits is not possible. So we have examined the physical evidence and developed a theory on what improved the outgassing during the reflow process.
Our theory is depicted in FIGURE 3. We believe that, because the I/Os are on the perimeter, they reach liquidus temperature before the center pad. As they melt, the overprints coalesce onto the I/O pads, lifting the component for a very short period of time – the time between the outside melting and the inside melting. As soon as the print on the center pad melts and wets, the package collapses the solder. We think momentarily lifting the lid formed by the component enables rapid outgassing, and/or the collapse of the component itself forces gas out as it compresses the liquid solder underneath it.
In our experiments, the standoff height appeared to be set by the center pad. Different overprint lengths did not substantially affect standoff heights. The extra solder printed on the I/O pads migrated to the toes and is visible as darker areas on the x-rays. We created 5,760 solder joints in this last run, and no bridging or solder balling was observed on any of the devices, even with the 30mil I/O overprint.
We deliberately didn’t do anything fancy on these tests. We used our standard test materials and setup, with a popular Type 4, no-clean SAC 305 solder paste, printed with a 4 mil (100µm) premium stainless steel stencil with a fluoropolymer nanocoating on our usual PCB2009 test board. A ramp-to-spike, or linear, profile was used. Most void-reducing reflow profiles incorporate prolonged thermal exposure or soak zones to promote flux volatilization prior to the alloy reaching liquidus temperatures. The goal of this study was to isolate and assess the efficacy of the I/O paste overprint; therefore, we used the least-forgiving thermal profile.
X-ray results were analyzed both visually and with statistical software. FIGURE 4 shows the pictures and the data for the 48 I/O QFN. For me, seeing is believing, and I think the x-rays offer the most convincing visual evidence that this technique works well at void mitigation. The statistics quantify the impact of the I/O overprint on voiding rates, reinforcing the visual images with solid numbers.
Armed with this compelling data, we are embarking on host of analyses and experiments. We are looking at mathematical relationships, theoretical height differentials, component masses, solid solder volumes, and ratios of pad areas, volumes and fillet lines. More areas to investigate come to mind almost every day. And we’re busy designing the next experiment:
We are excited to continue evolving this technique, as it is currently in its infancy. We have a lot to learn about it, particularly in terms of design optimization.
So that’s it. No need for costly preforms or elaborate profiles or inert reflow atmospheres. Simply increasing the volume on the I/O pads may hold the key to one of the most effective and easy-to-use voiding remedies, one that provides a significant improvement to arguably the most common frustration on every SMT production floor around the world. And, best of all, it’s free!
And now a blatant plug for the upcoming Apex conference, where we will present more details and the data behind this study. If this technique works as well on a production floor as in the study, it will solve a common industry challenge. Let’s discuss this in San Diego!